Field Validation of Thermoelectric Generation System at Holcim Cement Plant in Alpena, Michigan
| Publication Type | Report
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https://doi.org/10.20357/B7H60P
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| Abstract |
Executive SummaryProject BackgroundThe Industrial Technology Validation (ITV) program aims to identify and demonstrate the performance of new, emerging, and underutilized energy-saving technologies in the industrial sector to help inform decisions to help accelerate their commercialization and deployment, as well as to help make industries more competitive. This ITV demonstration evaluated a thermoelectric generation (TEG) technology at a cement plant, aiming to reduce energy demand in the cement industry. A median cement plant consumes 5.73 million British thermal units per ton of clinker production (resulting in 0.838 metric tons of carbon dioxide [CO2] emissions per ton of clinker) (Boyd and Zhang 2011, EPA 2021), equivalent to approximately 6.9 trillion British thermal units (TBtu) per year in energy consumption at a cement plant producing 3,300 tons of clinker per day.1 Collaborating with Holcim, Advanced Thermovoltaic Systems (ATS) developed and deployed a pilot-scale thermoelectric power system to efficiently capture and convert waste heat to electricity. The system leverages the Seebeck effect to convert temperature differences on two sides of semiconductor cartridges into electrical power (ScienceDirect, n.d.). This generation is realized with minimal moving parts compared to existing waste-heat-to-generation solutions and allows capture from heat sources with temperatures as low as 150°C. This project aimed to validate a scalable solution applicable for capturing medium-temperature waste heat, including ambient losses from other high-temperature processes, and high-temperature sources less suitable for other waste-heat-to-power solutions. By recovering this otherwise wasted heat, this project intends to validate improvements to overall process efficiency through reduction in purchased electricity, thereby reducing operational costs while enhancing resiliency and competitiveness. Description and ScopeThis study evaluated the performance of a TEG system from ATS as a solution to convert waste heat into useful power at a Holcim cement plant in Alpena, Michigan. This plant is a fully integrated cement plant that has been operating since 1907. The facility operates continuously (24/7/365) with approximately 250 employees and five long dry kilns, yielding a total production capacity of 7,852 tons of cement per day (EPA 2023). Currently, the Alpena plant uses waste heat boilers to convert waste heat from the exhaust of each kiln into steam, which drives steam turbine generators. The ATS TEG is being evaluated for its potential to supplement the steam turbines by capturing the remaining lower grade heat. This technology is also being considered for other Holcim plants where steam turbines are not a viable option. ATS installed a pilot-scale TEG unit with an array of 582 individual thermoelectric semiconductor cartridges, of which 573 were operational. The cartridges are sandwiched between 48 hot plates and 49 cold plates. Each cartridge is designed to generate 20 watts (W) of gross power at a hot-side temperature of 240°C and cold-side temperature of 20°C. As such, the total gross generation capacity of the installed system is 11.5 kilowatts (kW) at design conditions. The system configuration for the evaluation was designed to prioritize convenience of installation and minimize disruption to production at the site, while ensuring that the heat required can be obtained for evaluating the TEG system at various operational conditions. To accomplish this, a portion of the steam supplied to Alpena’s steam turbine generation system was diverted to be used as the heat source for the TEG system, while water was supplied to the cold side of the system from nearby Lake Huron. This configuration was designed for the evaluation of the pilot-scale system to assess the performance at different conditions. A commercial-scale system will likely vary from the pilot system depending on typical configurations, including both scale and application. Future commercial applications of the ATS system would involve integrating the system into the exhaust from kiln preheaters, clinker coolers, or radiant heat capture from kiln shells for the heat source. For the cold source, a range of cooling solutions can be considered, including a mechanical cooling system, depending on the location and the application. To increase the generation capacity for commercial applications, the technology provider is working toward developing a commercial scale TEG system, which would combine multiple TEG units (each similar in design to the pilot system) together. The scope of this evaluation includes the pilot-scale TEG system and all impacted equipment including pumps, controllers, and power handling equipment. Study ObjectivesThe evaluation's goal was to assess the potential of the ATS TEG system to generate useful electrical power by capturing waste heat from cement production kilns. The objectives of this study are to evaluate and verify the following claims made by ATS regarding the pilot-scale system installed at the Holcim Alpena plant. The following design parameters and claims are also outlined in Table ES- 1 and Table ES- 2:
In addition to evaluating the claimed performance of the TEG pilot-scale unit, the study estimated the potential annual impacts of a scaled-up commercial system used to capture kiln waste heat over annual operations. The evaluation estimated the gross and net annual electric generation achievable by capturing heat from the two proposed tap-in points: the kiln exhaust and the clinker cooler exhaust; see Section 2.1 for details. Two use cases were examined:
MethodologyThe evaluation methodology followed a measurement and verification (M&V) strategy based on the International Performance Measurement and Verification Protocol Option B through comprehensive measurements and analyses of the affected systems. Evaluation data was collected from March 9 to March 11, 2024, the test period of the pilot TEG system. During the test period, in coordination with the ITV team, the ATS team adjusted system operations to capture the range of variability expected for each of the variables pertinent to performance of the system. The methodology consisted of two parts: evaluating the performance of the pilot unit's TEG system and estimating the annual TEG impact in terms of gross and net power based on a given waste heat profile. First, the evaluation of the thermoelectric generation performance of the pilot unit relative to the claims was performed by analyzing the collected test data. Gross power of the pilot TEG system was directly measured. Net power was determined by deducting the measured parasitic power from the gross power. The gross power generation was compared to heat transferred to the system by the working fluid (which was heated by steam generated from the kiln waste heat) to calculate the thermal efficiency achieved by the system. Performance of individual semiconductor cartridges within the pilot array was also assessed in terms of measured gross cartridge power and calculated cartridge thermal efficiency. The second part of the evaluation estimated the annual TEG impacts in terms of gross power and net power (calculated from the difference between gross power and parasitic power). This analysis comprised development of mathematical regression models for gross power and parasitic power, with assessment of each model’s goodness-of-fit characteristics to ensure satisfaction of statistical requirements. The models predicted the gross power generation, the parasitic load based on the temperature difference between the hot working fluid and the cold side fluid (cold water from Lake Huron) entering the system, the volumetric flow rate of the cold side fluid at the inlet, and the volumetric flow rate of the hot working fluid at the inlet. The annual impact analysis considered a theoretical commercial-scale system sized to capture the available waste heat at a cement plant, consisting of linked pilot-scale units that receive heat from a theoretical gas-to-working-fluid heat exchanger. To estimate annual impacts at the Alpena plant, the gross power and parasitic power regression models were applied to the arrays in the theoretical commercial-scale system. The heat supplied to the unit was calculated based on the kiln run time, annual production, kiln exhaust waste heat, and clinker cooler waste heat derived from 2023 Holcim Alpena kiln operational data. Net power impacts were calculated by deducting the resulting parasitic power from the estimated gross power. Inputs for the model were generated from a combination of hourly data, assumed design considerations for TEG system scale-up from the pilot-scale unit, and assumptions regarding TEG system operations. This analysis was then used as the basis for estimating annual impacts of typical TEG installation at cement plants, by applying sensitivity analyses to key kiln operational characteristics including kiln preheater exhaust temperatures, cooler clinker exhaust temperatures, and plant daily production rates across a range of expected values. Project Results/FindingsTable ES- 2 and Table ES- 2 provide a summary of the operating conditions and evaluation results compared to the stated claims from the technology provider. Key takeaways include:
The regression models developed for gross power generation and parasitic loads were used to estimate the generation impact for given heat input to the TEG from the working fluid (captured from the waste heat) and from the cold loop (Lake Huron) on an hourly basis for a year of operation. Based on this analysis, installation of a commercial-scale TEG system at the Holcim cement plant in Alpena, Michigan, with a waste heat exchanger of 0.85 effectiveness, would generate up to 391 kW of net power, translating to between 920,000 and 1,800,000 kilowatt hours (kWh) in net electricity per year. Based on typical grid emissions for Alpena, this would avoid estimated net emissions by 752 metric tons of CO2 annually.2 The sensitivity analysis estimated that typical TEG system installations at cement plants could generate an average of 56–1,040 kW of net power, or between 488,000 and 9,110,000 kWh of net energy. This generation potential is most significantly affected by plant production rates and also influenced by preheater and clinker cooler exhaust temperatures. Applying the national average emission rate, typical commercial-scale installations at Holcim plants are projected to avoid between 182 and 3,401 metric tons of CO2 annually per site. Table ES- 3 shows a summary of the estimated annual impacts.3 While parasitic loads are significant and vary by application, this analysis assumed the use of heating loop pumps and access to Lake Huron as a cold sink. This setup assumed no need for cooling loop pumps due to the available water pressure at the test site. Applications that require cooling towers or additional equipment are likely to experience higher parasitic loads. Therefore, the study’s estimates are most applicable to scenarios with similar parasitic load configurations—namely, access to a high-pressure cold sink. Applicability to other locations may be limited, as differing conditions could necessitate additional pumps and cooling systems, potentially impacting performance significantly. |
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2025
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